ARC WELDER FROM A SINGLE TRANSFORMER

 

Having the need for a really powerful electric arc welder and not the ready cash to run out and buy a new one, we considered constructing one, since there seems to be little inside a welder other than a transformer and occasionally a fan.  Below, is pictured the inside of a 120 Amp AC hobby welder with its 22lb transformer.

 

 

 

Several such projects are to be found on the net, using such things as a bank of 8 MOT’s.  Seeking a simpler approach and having a supply of several large (40lb.) transformers salvaged from old IBM 5360 mainframe computers and x-ray control consoles; we decided to make this a snow day project.

 

The transformer chosen seemed ideal for several reasons.  First, this 41 lb. transformer was wired with a stout 240 VAC primary, large shunts, and multiple secondaries (some wound with #8 wire and even 3” wide copper sheet).  These were intended to deliver between 5 and 12 volts at upwards of 100 Amps for the huge disk drives and power hungry boards of these old computers.

 

 

Considerable space was evident between the secondaries and the frame.  The removal of the secondaries, however, is every bit the noisesome a chore as reported by others.  We first spent a good hour letting a metal band saw eat down through the windings protruding from one side.  This got us within a bout ½” from the bottom of the secondary windings when tension broke the band saw blade!  Not to be daunted by minor setbacks, we spent the next hour or so with a hammer, chisel, screwdriver, wire clippers, and even a large bolt cutter.   Ultimately, this brute gave up its last winding, leaving sore fingers and a considerable mess on the shop floor.  The huge vacant space revealed will allow the use of #4 or even #2 THHN for the secondary rewind.  The magnetic shunts were then tapped out.

 

 

 

This was the main base transformer for the 5360.  This 1985 era mainframe was wired for 240 VAC 20 Amp service for the base unit with no expansion cabinets.  Assuming about 15 Amp average current draw, the primary was around 3600 VA.  At 100% efficiency, this would support up to a whopping 720 Amps at 5 Volts on the secondary (360A @ 10V, 300A @ 12V, 180A @ 20V, and 150A @ 24V).  We decided to shoot for the 10-12 Volt no load secondary at 300-360 Amps with the knowledge that the heavy load of arc welding would drop this to between 2 and 4 Volts nominal.  The primary consists of about 150 turns of #12 magnet wire.  Approximately 6-8 turns on the secondary would give the appropriate voltage reduction. 

 

Desiring to use the largest AWG possible due to the output current and the fact that magnet wire of extremely heavy gauge is out of the question from an expense standpoint, our choice was between #4 and #2 THHN.  The cost difference of 10¢ per foot  made the use of #2 AWG at 59¢ per foot the obvious choice and 15 feet was more than enough.  Rewinding with #2 THHN proved a considerable challenge given its size and lack of flexibility, but half an hour of strenuous effort closely resembling alligator wrestling resulted in 6 turns of wire in place – after a fashion.  I doubt there is any way to get a ‘tight’ wind with something this big.   The heavy insulation was not damaged but the thin shiny dress coating was shredded in few places from the unavoidable friction of pulling the heavy wire through the frame. 

 

Output voltage was measured at a little over 10 volts at the secondary with 246 Volts in at the primary.  A mild hum was produced when the unit was powered up with no load.  Shorting the secondary instantly melted the end of the copper wire and almost brought the transformer up off of the floor; so it appears we have a winner here – easily capable of sustaining welding level currents.  The relatively light 30 Amp fusing on the circuit was unharmed.  Due to the considerable excess of THHN, 2 more windings were later added, which brought secondary voltage to about 13.5 Volts.  The thought behind this was that windings can always be removed if the additional 3 volts proves problematic, but adding more once the #2 was cut off would be next to impossible.

 

As a sort of preliminary test to insure that we were heading down the correct path, battery jumper cable clamps were installed on the ends of each output lead.  A 9” length of standard steel coat hanger was secured into one clamp and the other was clamped onto a piece of ¼” plate steel.  The unit was energized and rod brought into contact with the work briefly as a single tap.  The resulting spray of sparks was quite satisfactory.  The rod, however, had turned incandescent red over its entire length.  A second tap bought the rod to a bright yellow-orange color, persisting even after contact was broken.  An attempt at that point strike an arc and draw a short bead across the work surface immediately brought the steel wire to white heat followed by complete liquefaction of the entire steel rod - the resulting puddles of liquid steel running across the work surface. Inspection after de-energizing the unit found the transformer and cables not even warm.

 

 

With the addition of a heavy duty SCR and a control circuit for its gate, we hoped to gain the ability to choose between AC, +DC, or –DC type welding. An NTE 5588, 1600 Volt PIV, 355 Amp average forward current, 5000 Amp peak surge current, SCR was in one of the parts bins. Since SCR’s emit 1.5 Watt as heat for every Ampere conducted, up to 600 Watts may need to be dissipated. For this reason, it was mounted on a large heatsink with a 240V Muffin Fan directed across it.

 

 

 

Gate trigger voltage for this SCR is between 0.25 and 3.0 Volts. Preferring an isolated control circuit, about 5-6 turns of #14 AWG THHN were wound around the transformer center leg, giving about 8 Volts that dropped to 6 VDC when pushed through a full wave bridge rectifier.   A 2-stage filter was then connected to smooth the DC ripple.  This circuit was connected between the gate and cathode of the SCR to provide a flat and stiff DC current that keeps the gate triggered to the on-state. Below, is the schematic.

 

 

FAILURE!

 

Although the foregoing design and experiment seemed promising, the results did not bear out the theory as expected.  We were simply not able to generate high enough current levels to be useful despite the theoretical potential.  Postmortem analysis reveals the inability to get the heavy wire wound snugly against the transformer frame resulted in tremendous efficiency loss.  The magnetic field drops off sharply by the Law of Inverse Squares and the field lines were just not strong enough an inch or so out from the frame to induce significant current.

 

The second factor was not so apparent and only surfaced after speaking with a local authority on welding.  The output voltage chosen turned out to be way too low.  It was based on my reading of several hobby websites which seemed to indicate that welders should output around 10 volts with no load and drop to below 5 volts during welding.  We obtained the use of a small arc welder for comparison, and to our considerable surprise, its output no load voltage was 45-50 Volts which dropped to 18-20 Volts during welding.  This corroborated what the welding specialist had said.  No doubt it was time to return to the old drawing board.

 

One possible solution was considered and rejected for cost reasons.  It seemed fairly obvious that removing our secondary and rewinding tightly with very large magnet wire and 4 times the number of windings would probably solve the problems.  However, a cursory examination of sites offering magnet wire revealed that the cutoff is around #12 for most companies though we did find one site that offers #8 wire.  Further, the cost per pound is high and a pound of the big stuff is only a few feet.

 

In the interim, a novel solution presented itself.  We have a number of large to very large (30 to 150 lbs.) autotransformers lying around collecting dust.  I examined one in the 55-60 lb. range to find that it was entirely wound with stout magnet wire of at least #8 AWG.  Consulting the schematic, I discovered it was designed for input voltages between 220 and 260 Volts to give an output of 0-300 VAC full scale and handled a couple hundred Amps in the equipment from which it was removed.  It was provided with 17 output taps over that range.  

 

 

Since output voltage of an autotransformer is directly proportional to its coil length, we postulated that it should be possible to calculate the results of converting it to a traditional type transformer by splitting the coil into 2 coils – a primary and a secondary - at one of the tap positions.  With 245 Volts as the intended primary input voltage, a transformation ratio of 1 in 10 would yield a secondary out put of 24.5, which is exactly half of the 49 Volts desired.  Therefore, a turns ratio of 2 in 10 is then what is needed.

 

Assuming the autotransformer to be relatively uniform in winding, then the tap with a designated output voltage closest to 80% of the full scale voltage is where the coil should be severed.  Since 80% of 300 is 240, the tap at 238 Volts was chosen.  The protective covering was removed and the tap loop cut at its center.  Continuity check with the DMM resolved the identities of the new primary and secondary.  The primary was then energized and the voltage ramped up slowly with a Variac until it reached 120 VAC.  The output of the secondary was exactly 24.5 Volts!  It followed then that when we switched to a 240 VAC source, we would have the 49 Volts we were seeking.

 

The only noticeable drawback to this new design was that the autotransformer had no place for the insertion of shunts to control the output current.  Two solutions came to mind.  The first would have been to have designed some type of electronic modulation circuit – interesting but complicated.  Another approach would have been to have rewinded our first transformer with magnet wire, shorted the secondary, installed large adjustable shunts, and put the primary in series with the input line to this new transformer.  This would have been a variable inductor to control input current draw.  And since we know that power in on a transformer equals approximately power out, this would in turn have regulated the output current.

 

 

 

As it turned out, we certainly needed a heavy duty current control method for this brute.  Full power testing was done by  shorting the secondary and applying 240 VAC to the primary.  The first source circuit had 30 Amp max and the breaker instantaneously tripped before the current clamp on the secondary could give a reading.  The primary was then energized using a 50 Amp circuit.  It took about 1-2 seconds before the tremendous heat melted a soldered lead and broke the circuit, but not before the current meter displayed 585 Amps. Wow!!! 

 

If VApri = VAsec at 100% efficiency (probably more like 92-95% in reality but we will ignore this), we have 240 (X) = 50 (585).  Primary draw may have been on the order of 100-150 Amps and would most certainly have tripped the breaker if the circuit had not failed first.  This, of course, is way beyond useful welding current and had to be throttled back.  The first step was to place a current limiting inductor in the input line capable of withstanding the savage power draw.  We have a 22 lb. dual scale adjustable inductor that has a reactance range of 66 to 71 Ohms on one scale and 7.5 to 28.5 Ohms on the second and more useful scale.  Using this second range, we able to limit the current draw to between 8.4 and 32 Amps thus allowing comparison with output current to find the exact relationship.  Once this was determined, a precision inductor was designed to allow adjustment of current in the useful welding range (50-250 Amps.).

 

With the resistance of the work and electrode substituted for the dead short above, the maximum secondary current was reduced to about 360 Amps.  The results of testing with the inductor showed that even at 7.5 Ohms reactance, the current reduction is still too great.  A maximum output current of around 60 Amps was obtained.  By placing a second inductor with a reactance of 4.5 Ohms in parallel, we obtained a low end output current of 120 Amps, which has no trouble welding plate steel. 

 

 

Now that we see that we have a successful welder, we will replace our experimental inductor with a permanent current control.  A small rotary tap autotransformer might give a workable solution but we were seeking a solid state solution to hold down the weight.  Unfortunately, multiple attempts to design a front end adjustable current control using a large dual SCR power module in a circuit resembling a light dimmer failed.  The circuit would control voltage in the same manner as a light dimmer to a small resistive load (actually a light bulb) but had no effect on current draw to the primary of our welder other than to act as an off/on switch at the limit of the potentiometer.

 

Multiple examples of inductive ballast were tried with the expected range of variation in current control.  We finally settled on a small 10-tap autotransformer that resembles a tiny version of the power transformer.  The rotary tap switch was still connected to the taps and the weight and footprint are small.  Under actual welding conditions, the measured secondary current for the 10 settings ran from about 30 amps to about 190 Amps.

 

 

The external cables for welding were constructed of #1/0 AWG welding cable of about 12 foot length each.  To one was connected a 600 Amp ground clamp:

 

Powerweld® Ground Clamp Screw Type 600 Amp GCC600

 

To the other, a 300 Amp electrode holder:

 

Powerweld® Electrode Holder 200 - 300 Amp interchangeable w/ Tweco®

 

the AC, DC, and Common connections to the unit were made via removable interlocking LC-40 type connectors:

 

Powerweld® Cable Connector LC-10 #6 - #1 Cable interchangeable w/ Lenco®

 

This fun and instructive project set out to build a useful welder with a single salvage transformer.  We ultimately had to use a second much smaller transformer as ballast but in essence we have accomplished what we set out to do.

 

 

The 60 Hz half wave pulse from the SCR did not give smooth results for +/- DC welding.  For this reason, we to replace decided this rectification method with a full-wave bridge.  The SCR, heatsink, and computer power supply 5 Volt source were removed.  Our inventory of diodes/thyrisors included a half dozen or so GE A 71PB diodes.  These are basically equivalent to JEDEC # 1N3296 and we have both standard and reverse polarity types.  These have a average forward current rating of IAF = 125A  and therefore an RMS or continuous on-state tolerance of IRMS = 250A, which is also a peak of IPK = 350 Amps.  The momentary surge rating is 2000 Amps and PIV is 1200 Volts.

 

 

Two large solid aluminum heatsinks were tapped at each end for the threads of the diode studs and a pair of standard polarity diodes were inserted into the ends of one and a pair of reverse polarity units into the other heatsink.  The heatsinks were mounted side-by-side about 2 inches apart.  The braided cathodes of the two diodes on one side were secured to the braided anodes of the diodes opposite them, creating the bridge.  AWG #2 THHN was run from either side of the transformer secondary to one of the afore-mentioned connections, providing the AC input to the bridge. 

 

 

This then makes the heatsinks themselves the positive and negative output terminals.   Additional # 2 THHN was run from each heatsink to the LC-40 female output connectors on the front plate and labeled + and – respectively.  The 3rd LC-40 female was connected back to secondary of the transformer with #2, bypassing the bridge, to provide one permanent AC welding connection.  Should AC welding become desirable for some reason, a shunt is placed across one of the DC lines to also bypass the rectifier and provide the other AC leg.

 

 

Both DCEP (DC+ or DC reverse) and DCEN (DC- or straight DC) welding were tested over the entire range of current and the results were excellent and as expected.  The bead below was produced on the surface of a 1/4” thick steel channel using a 1/8” diameter E6013 rod on DC+ at about 100 Amps. 

 

 

In high-power AC mode at around 360 Amps, the metal fairly explodes when the rod is brought into contact.  Sheet metal is cut completely through even with a surface rod like E6013.  The eighth inch rod, however, is unable to stand the tremendous heat generated.  After about 1 foot of cut, the rod becomes cherry red and will melt completely if an attempt is made to use further before it cools.  Obviously, a heavier rod or gouging setup is indicated at these current levels.

 

 

 

We later came into possession of several monster diodes that have an average continuous forward current rating of 300 Amps (nearly 600 Amps RMS) and a maximum repetitive peak current of 1400 Amps!. We could not resist rebuilding the the rectifier bridge to incorporate these into the design 

 

 

The control circuit was added on a smaller second level board. The 'OVERDRIVE' switch supplies 240 volts to the 20:1 step down transformer. Its 12 Volt output is rectified and supplied to the coil of the high current relay to switch the adjustable inductor loop in or out of one leg of the primary input line. We had a 600 Amp to 5 Amp current transformer but our meter was 300:5. Using these 2 together necessitated changing the scale on the meter. As a temporary measure, the numeric decals seen in the photo were placed meter cover. 

 

 

The above welder has been such a successful project and enormously useful tool that we decided to make another unit and go as large we possibly could with materials on hand. Our largest autotransformer weighs a little over 150 lbs. Wound with AWG 6 magnet wire, it was intended for up to 400 Amp service. We split the winding at a tap that gave 72 Volts open circuit on the secondary at a maximum of over 450 Amps output when 240 Volts is applied to the primary. The primary current draw is less than 100 Amps. Below, is a photo of the transformer and secondary output curcuit set into the steel frame made up with the welder contructed above. 

 

 

In the next view below, the secondary circuit is seen from above. The secondary output is taken from the transformer using heavy aluminum block connectors with set screws. The wiring to the aluminum blocks on the board is AWG 4 bare copper. A current transformer will be placed around one of these and run to an ammeter on the front panel. The output is then taken to the rectifier bridge using AWG 2 stranded THHN. 

 

 

Below, is a closeup of the rectifier bridge. We were able to acquire some very high current diodes at a price so low that we couldn't pass them up. They are Ruttonsha 300 UM 120 diodes − 2 standard and 2 reverse polarity types. These have a 1200 Volt PIV and forward current average of 300 Amps (about 450 RMS Amps), with a repetitve forward current maximum of 1400 Amps. Two standard polarity diodes were inserted into one heatsink and 2 reverse polarity diodes into the other. The braided terminals were connected between pairs to form the bridge and the input is to these connections. This arrangement then renders the heatsinks themselves as the positive and negative output terminals for the unit. 

 

 

 

A second tier will be added to contain the control circuitry. In this unit, output current is controlled with a solid state control curcuit on the primary side. It was built around a high current dual SCR block with adjustable gating. This circuit is pictured below. 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

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